Production
pressures, limited resource availability, the lack of detailed process
equipment knowledge, and the costs associated with equipment downtime
often lead semiconductor fabs to adopt a symptom-treatment approach
to handling process equipmentrelated particle problems. Sudden
particle excursions during production are frequently alleviated
by simply repeating a particle check or by performing a chamber
purge or cleaning step. The drawback to this approach is that another
particle event with the same root cause is probable. This risk can
be minimized by the establishment of partnerships between chip manufacturers
and their equipment vendors. Supplier service programs at customer
manufacturing sites can range from collaborations with the fab's
factory service organization to full ownership of equipment.
After
an equipment-related particle event at a fab is identified and confirmed,
a process-monitoring phase is initiated to fingerprint the suspect
process tool. Following the collection of wafer monitor results,
those data that reveal typical defect types, trends, or signatures
are extracted and correlated. (In most of the cases discussed here,
this analysis phase relied heavily on the capability of a scanning
electron microscopy [SEM] system to extract information on defect
size, morphology, and composition.1) The next step involves
particle characterization and root-cause analysis performed by process
and equipment engineers from the tool supplier, who utilize their
company's so-called defect knowledge library to search for descriptions
of similar excursions.2 That library is a database containing
descriptions of process toolrelated defect problems that have
been documented, and resolved, in the past. In the final phase,
corrective action is followed by a second process-monitoring phase
to confirm that the appropriate solution has been implemented.
This
article focuses on the successful implementation of a partnership
between two Philips Semiconductors fabs and Applied Materials Europe
(Nijmegen, The Netherlands). The methodical approach to identifying
and resolving the root causes of particle events in collaboration
with the toolmaker is described, and examples of applying the methodology
in three process domainsoxide etch, ion implant, and metal PVDare
provided.
Enhancing
Oxide Etch Chamber Productivity
One
productivity enhancement program at Philips Semiconductors' Böblingen,
Germany, facility focused on a series of identical MxP+ oxide etch
chambers from Applied Materials (Santa Clara, CA) that are used
for contact and via etch of customized logic devices, including
analog options, LCD drivers, and embedded DRAMs at technology nodes
down to 0.32 µm. It had been noted that a number of the chambers
were running below their intrinsic productivity level, which translated
into an elevated percentage of out-of-control first particle measurements.
The performance of the etch chambers at the beginning of the program
is shown in Figure 1, which also indicates the average and specification
values. The initial approach to improving the productivity level
on the underperforming chambers was to refer to a set of "golden
system" chambers and try to match the particle behavior of those
chambers.
 |
| Figure 1: Particle performance
of selected oxide etch chambers at the start of the productivity
enhancement project (percentage of first particle measurements
within the specification of <120 adders). |
Selected
system chambers were monitored initially, but very few particle
excursions were encountered. Therefore, a significantly larger set
of chambers was monitored to enable quicker identification of the
causes of the particle events. This expanded effort made it clear
that many of the excursions were genericthat is, they might occur
on any of the identical process chambers at any given moment in
time. Thus, it was decided that the way to proceed was to identify
as many different particle excursion modes as possible and implement
respective corrective actions on all of the chambers. This approach
led to a steady improvement of productivity across the oxide etch
systems. Examples of some of the excursion modes that were eliminated
are discussed below.
Arcing.
One type of particle excursion was traced to an arcing problem.
Particle measurements performed on monitor wafers showed a progressively
higher particle count over time for one particular process chamber.
In addition, map analysis demonstrated that the particle distribution
changed from an initial quasi-random pattern to a very specific
signature with most of the defects near the wafer edge, as shown
in Figure 2. Defect review and energy dispersive x-ray (EDX) characterization
using a SEMVision defect review system from Applied Materials revealed
that there were three distinct contamination phases, as depicted
in Figure 3. At baseline, mainly small (≤1-µm) SiO2
particles were detected. When the first particle excursion measurements
appeared, spherical submicron-sized aluminum oxide (AlO) particles
began to be detected along the wafer edge. Finally, large (>1-µm)
aluminum fluoride (AlF) particles were detected, indicating a gradual
buildup of contamination in the process chamber.
 |
|
Figure
2: Wafer defect maps from inspections of monitor wafers processed
on an oxide etch chamber, illustrating that particle levels
increased over time, with many particles near the wafer edge.
Measurements were taken on (a) May 4, (b) May 7, (c) May 10,
(d) May 11, and (e) May 15.
|
The
particles' composition (aluminum) and distribution (at the wafer
edge) suggested that their root cause was arcing at the backside
of the wafer. Further analysis of monitor wafers processed in the
etch chamber confirmed this theory, revealing traces of backside
arcing at a position coincident with a lift-pin position. An examination
of the lift pins showed one to be worn and arced, and subsequent
replacement and alignment of the pins eliminated this particle excursion
mode.
Nonoptimal
Parameter Settings. A second excursion mode involved another
oxide etch chamber that had yielded frequent out-of-control first
particle measurements. Wafer inspection and defect review analysis
indicated that most particles added during the oxide etch step were
quartz. However, in this case, the information on defect counts,
signatures, and composition did not provide a direct indication
of the problem's root cause.
 |
|
Figure
3: Summary of SEM-based defect review and EDX analysis data
for oxide etch monitor wafers over time.
|
A
review of the radio frequency (RF) recipe used for particle performance
verification revealed that the gas used for this step was not optimal,
but changing to the commonly used mixture of CF4
and CHF3/O2 led initially
to even-more-severe particle excursions. Two types of particles
were detected: aluminum (40%) and quartz (50%). Examples of the
honeycomb-shaped aluminum particles are shown in Figure 4.
 |
|
Figure
4: SEM images of honeycomb-shaped aluminum particles detected
on monitor wafers for oxide etch recipe with non-BKM parameter
settings. Field of view is 4 µm.
|
Further
investigation demonstrated that several tool parameter settings
deviated significantly from those in the best known method (BKM)
recipe. The most pronounced deviation was in the RF power ramp-down
time, which was longer than the BKM specification. Full implementation
of the BKM recipe resulted in a strong reduction of the number of
added particles, as shown in Figure 5. The effect of the non-BKM
settings on particle performance was confirmed on another etch chamber.
Monitor wafers processed in that chamber using the same non-BKM
settings also contained a large number of honeycomb-shaped aluminum
particles. Because the morphology of these particles was unusual,
that information was included when the excursion and its solution
were documented in the tool vendor's defect knowledge library.
 |
|
Figure
5: Particle performance as determined by delta count measurements
before and after implementation of BKM parameter settings
in the oxide etch recipe.
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Particle
Backflow. Another excursion mode was related to particle backflow
during periods of chamber inactivity. Particle test failures at
start-up had been observed consistently on a chamber that was not
used continuously for production, although no excursions had been
noted when particle checks were performed immediately following
its use. In this case, implementation of a reactor laminar flow,
which minimizes the effect of particle backflow from the pumpline,
resulted in a significant decrease in the particle excursion frequency,
as shown in Figure 6.
 |
| Figure 6: Particle measurement
data for an oxide etch chamber before and after implementation
of a reactor laminar flow (RLF) to prevent particle backflow
from the pumpline during periods of inactivity. Target specification
is <10%. |
Eliminating
a Defect Pattern on Implanted Wafers
Another
project carried out at the Böblingen fab investigated a defect
problem encountered on product wafers following processing on a
batch-type ion implanter. Several wafers (typically four or five)
of each 17-wafer batch suffered from a spatial defect pattern that
was not related to a specific position on the implant wheel. In
addition, all of the wafers processed in the batches containing
affected wafers suffered from high background particle levels. Figure
7 shows a typical defect map of a wafer that exhibited both the
pattern and a high defect density. Because wafers in one of the
fab's process flows require three different implants on this type
of system, overall process-line yield was being significantly affected,
as illustrated in Figure 8.
 |
|
Figure
7: Example of the defect signature observed on an implanted
wafer. (The wafer was intentionally rotated prior to implant
by 180°.) Also shown is a projection of the implant tool's
inner gripper (red dashed-line circle) and magnified view
of the defect cluster in the solid-line circle.
|
Detailed
EDX analysis of the detected defects indicated that the particles
did not contain any metal, thereby eliminating the investigators'
initial suspicion of arcing as the problem's root cause. Most particles
were silicon or carbon fluoride.
A
more-detailed analysis of the wafer maps revealed that the signature
pattern appeared to be a segment of a circle (as illustrated in
the magnified portion of the wafer map in Figure 7). A review of
the implant system's component configuration by a hardware expert
revealed that the radius of this circle exactly matched that of
the inner gripper plate used to place the wafers on the implant
wheel (represented by the dashed-line circle in Figure 7). This
hypothesis, which suggested that the particle problem was related
to the wafer-handling unit, was confirmed when the defect signature
disappeared after the inner gripper plate was replaced by a dummy.
A
closer examination of the gripper's performance revealed that overshooting
occasionally occurred, resulting in contact between the wafer surface
and the plate. Subsequent adjustment of the gripper hardware permanently
solved the particle problem; the original gripper plate was reinserted
without further particle excursions. In addition, after the gripper
hardware was optimized, the background defect density on all processed
wafers was maintained at the baseline level.
Reducing
Postsputtering Defect-Density Levels in a Metal PVD Process
A
third project, undertaken at the Philips Semiconductors MOS4YOU
fab (Nijmegen), focused on Endura PVD titanium (Ti) sputtering tools
from Applied Materials. These PVD systems are used to manufacture
logic devices with options, including nonvolatile memory, at technology
nodes down to 0.15 µm. A recent equipment defectivity evaluation
at the facility had found that median defect-density levels following
Ti sputtering were significantly higher than the benchmark. Thus,
the main goal of the project was to return to and maintain the benchmark
level.
The
fab's bare-wafer production-monitoring scheme used a 6420 double
dark-field tool from KLA-Tencor (San Jose) before and after Ti sputtering,
resulting in a differential defect count. A new scheme, in contrast,
used a more sensitive WF-736 dark-field inspection system from Applied
Materials to compare wafer defect maps obtained before and after
Ti sputtering, resulting in true adder data. This capability enabled
the investigators to focus their review and characterization efforts
on those defects added during processing.
 |
|
Figure
8: The impact of the ion implant system's poor particle performance
on process line yield (PLY) during the processing of lots
5166.
|
During
the project's initial monitoring phase, results based on the bare-wafer
production-monitoring scheme demonstrated that median defect- density
levels had returned to the benchmark for most of the Ti sputtering
systems. This finding can be attributed to the hardware adjustments
that were implemented immediately after completion of the equipment
defectivity evaluation. However, initial results using the state-of-the-art
dark-field monitoring scheme suggested that typically as many as
20 adders were detectable following the Ti sputtering step.
The
defect map comparisons also revealed that a significantly higher
number of defects were present on monitor wafers prior to sputtering
than after. SEM defect review and EDX analysis demonstrated that
the defects found on the monitor wafers prior to sputtering were
very similar in size, morphology, and composition to the true adders
(excluding the Ti component in the EDX spectra for the postprocess
particles) present after Ti sputtering.
 |
|
Figure
9: Schematic representation of the process flow of out-of-the-box
wafers used to monitor the Ti sputtering process (red circles)
and a simplified process flow that was used as a reference
(green circles).
|
In
contrast, analysis of monitor wafers processed directly out of the
box, which did not undergo any process steps before sputtering,
demonstrated that they had no defects before or after the Ti sputtering
process, as can be seen in the lower half of Figure 9. The out-of-the-box
wafers were processed together with standard monitor wafers, which
again were found to contain a high number of adder defects. These
results suggested that the defects detected on the monitor wafers
and identified as true adders were not, in fact, related to the
sputtering tool. In addition, many of those defects disappeared
during Ti sputtering, suggesting that they were mobile and that
most were previous-layer defects that had migrated during the sputtering
step. The decrease in small particles on the monitor wafers that
had been detected before the sputtering step may have been related
to the degas step of the monitoring sequence.
The
next step was to investigate the only two processes performed on
the standard monitor wafers prior to Ti sputtering: laser marking
and wet chemical cleaning (the standard RCA clean). Although the
laser marking process was shown to add a large number of particles
to the monitor wafers in some cases, the particles' size, morphology,
and distribution were not consistent with the defects that had been
observed previously before Ti sputtering. An additional test, in
which monitor wafers were processed only in the RCA-cleaning system,
demonstrated that this equipment was the source of the types of
particles observed on the monitor wafers before Ti sputtering.
The
fab's RCA-clean system processes four lots at a time, and the types
of defects present on the monitor wafers were found to vary depending
on the production lots that were cleaned with them. Two types of
particles were detected on the clean monitor wafers using SEM and
EDX analysis: submicron-sized (typically 0.30.5-µm) carbon
and carbon fluoride (CF) particles, and larger (>=1.0-µm)
CF and SiO2 particles. An example of each
type of particle is shown in Figure 10. The smaller particles were
typically observed when the monitor lots were processed with production
lots that received a resist strip after etch, while the larger particles
were seen on wafers processed with production lots that had undergone
oxide deposition. These results demonstrate that the RCA clean is
not fully efficient in removing particles and that cross-contamination
may occur when monitor lots are processed with production lots.
 |
|
Figure
10: Examples of defects typically detected on the monitor
wafers after RCA cleaning and prior to Ti sputtering: (a)
submicron-sized (0.3-µm) carbon particle detected when
the wafers were processed with production lots that received
a postetch resist strip, and (b) a larger (~1-µm) defect
detected on wafers cleaned with production lots that had undergone
oxide dielectric processing. Field of view is 2 µm for
(a) and 4 µm for (b).
|
Inspections
of monitor wafer maps using the state-of-the-art dark-field inspection
system revealed that the numbers of particles added during the RCA
clean varied greatly. Total postprocess counts reached as high as
1000 for the small carbon and CF particles, and a count of 10 was
typical for the larger CF and SiO2 particles.
Superimposing defect maps of monitor wafers processed in the RCA
cleaning equipment containing the smaller particles revealed a clear
spatial signature consisting of two defect lobes near the wafer
edge, as seen in Figure 11. This particle distribution is a consequence
of the rotational movement of the wafer cassettes during the RCA
clean. To address this issue, a program to improve the cleaning
tool has been implemented at MOS4YOU.
 |
|
Figure
11: Superimposed wafer maps of monitor wafers containing submicron-sized
carbon and CF particles. The resulting stacked map reveals
spatial defect signature consisting of lobes near the wafer
edge.
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Conclusion
Three
defect-reduction and productivity-enhancement projects carried out
at Philips Semiconductors showed the value of adopting a methodical
approach to process equipmentrelated particle contamination
problems. Such a methodology results in permanent solutions, not
just problem masking. SEM-based defect review and characterization
was found to play a central role in this approach, making it possible
to quickly identify main defect types and trends. The synergy of
process (equipment) and defect metrology knowledge developed by
the equipment manufacturer was shown to be advantageous in solving
equipment issues together with the chip manufacturer.
Acknowledgments
The
authors wish to thank the Applied Materials customer productivity
support and technology organizations in Nijmegen, The Netherlands,
and Böblingen, Germany, for their continuous support during
the defect reduction projects.
References
1. CR
Brundle and Yuri S Uritsky, "Particle and Defect Characterization,"
in Handbook of Silicon Semiconductor Metrology, ed. Alain
C Diebold (New York: Marcel Dekker, 2001), 550.
2. Jaim
Nulman, "Using Process Tool Automation to Increase Efficiency and
Productivity in 300 mm Factories," Semiconductor Fabtech
13 (March 2001): 245247.
Robert
Schreutelkamp, PhD, is a technologist in the Philips global
account team of Applied Materials Europe. Previously, he held positions
in applications and marketing for the company's process diagnostics
and control division. He received a PhD in physics from the University
of Utrecht, The Netherlands. (Schreutelkamp can be reached at +31
24 3512039 or robert_schreutelkamp@amat.com.)
Marc
van der Reijden is a process technologist in the Philips global
account team of Applied Materials Europe. He works in the areas
of etch and CVD. He received an MS degree in electrical engineering
from the Technical University of Twente, The Netherlands. (van der
Reijden can be reached at +31 24 3512014 or marc_reijden@amat.com.)
Tim
King is a process support engineer for metallization in the
Philips global account team of Applied Materials Europe. He has
worked for the company for 10 years in the fields of ion implant,
etch, PVD, RTP, and MCVD. Before joining the company, he worked
for Philips Semiconductors in The Netherlands and the UK, where
he was involved in development work in IC assembly techniques. (King
can be reached at +31 24 3512053 or tim_king@amat.com.)
Kristina
Mast, PhD, is a process engineer in the Philips global account
team of Applied Materials Europe. She is responsible for ion implantation
processes. She received a PhD in chemistry from the University of
Kaisers-lautern, Germany. (Mast can be reached at +31 24 3512064
or kristina_mast@amat.com.)
Jaap
Zondag is technology manager in the global Philips account team
of Applied Materials Europe. Previously, he worked in sales and
marketing for the company's Philips account group and the etch division.
Before joining Applied Materials, he worked at Philips Semiconductors
in Nijmegen as part of the bipolar process development group. (Zondag
can be reached at +31 24 3512026 or jaap_zondag@amat.com.)
Hartmut
Sahr is team leader of the etch group at Philips Semiconductors
in Böblingen, Germany. For more than 25 years he has been involved
in the semiconductor industry in the areas of hot equipment engineering,
CVD process engineering, and etch process engineering. In addition,
he spent two years on assignment at IBM in Burlington, VT, working
on semiconductor manufacturing projects. (Sahr can be reached at
+49 7031 185822 or hartmut.sahr@philips.com.)
Jan
Cavelaars is a senior process engineer in the metrology and
defect reduction group at Philips MOS4YOU wafer fab in Nijmegen,
The Netherlands, where he has worked since the facility started
up in 1995. His responsibilities include defect control strategies,
defect-related improvement programs, interface to defectivity operations,
maintenance of group procedures, and defect casebooks. Previously,
Cavelaars served as a tool owner of various defect metrology systems.
He received an MS in applied physics from Twente University of Technology,
The Netherlands, and undertook a two-year process and product designer's
course at the Technical University of Eindhoven, The Netherlands.
(Cavelaars can be reached at +31 24 3534393 or jan.cavelaars@philips.com.)
Mario
Swaanen is a process engineer for PVD metallization at the Philips
Semiconductors MOS4YOU fab in Nijmegen. He joined the company in
1995 as a process engineer for PVD metallization. From 1999 until
2001 he was a development engineer for advanced metallization at
STMicroelectronics in Crolles, France. (Swaanen can be reached at
+31 24 3535117 or mario.swaanen@philips.com.)
Liang
Shi, PhD, is section manager in the metrology and defect reduction
department at the Philips Semiconductors MOS4YOU fab in Nijmegen.
Previously, he held process integration and defectivity positions
at the fab and participated in 19961997 in a joint embedded
flash memory development program at TSMC (Hsinchu, Taiwan). Before
joining Philips Semiconductors, he held several technology positions
at Delft Instruments and Unilever. He received MS and PhD degrees
in applied physics from the Delft University of Technology, The
Netherlands, where he also spent several years in a postdoctoral
position in the area of InGaAsP-based optoelectronic devices for
optical communications. (Shi can be reached at +31 24 3534521 or
liang.shi@philips.com.)